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The Tube Project: |
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Search results for : (7) Sports
Very high (approx. 600 ft, 183 m) RC- helicopter flight with movable onboard camera. Very low inverted flying and high speed low pass. Crash caused by failed autorotation!
Vibration problem solved.
Setup: Standard Thunder Tiger Mini Titan E325
BLC-40 (Standard Motor Timing, No Brake, Fast Throttle Response, Standard Discharge Protection, Heli Mode Without Governor
Hacker A20-6XL
Kokam 2100 11,1V 30C H5
3x Thunder Tiger C1016
1x Futaba S3114
1x Hitec HS 55 for camera head movement
Robbe- Futaba GY-240
Align 315 Pro Main Rotor Blades (wooden)- get replaced by Hyperion 325 CFK Blades
Align Tail Rotor Blades for T-Rex 450 (plastic)
Graupner- JR MX-16S, 40 MHz
R16-SCAN
Approx. 2600 rpm at head
Weight 923 g with movable FlyCamOne2
Plastic rotor head gets replaced by an aluminum head
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